The big news is that I was unhappy with hesitation between 2 and 3 K RPM. I tried working on timing, new spark plugs, carburetor balancing and adjustment, but no significant improvement. Not being willing to tear down Weber carburetors I took it to a specialist who determined that the idle jests were too small. After they replaced the jets the hesitation was gone. So was spitting out of the carburetors and explosions out of the exhaust. It made a huge improvement to the drivability of the car. The only thing remaining is to deal with some smoke. Today was the last autocross of the season, so my plan is to pull the head, check the valve guides and seals, and take a look at the cylinders. What I can afford to fix I will fix over the winter.